TY - GEN
T1 - Improvement of productivity by applying 5S, Work Standardization, Ergonomic Analysis and Poka Yoke in Metalworking Company
AU - de Tramontana-Pinzás, Gianluca Rafael
AU - Shirota-Huchiyama, Luis Sadashige
AU - Corzo-Chavez, Jorge Antonio
N1 - Publisher Copyright:
© 2025 Latin American and Caribbean Consortium of Engineering Institutions. All rights reserved.
PY - 2025
Y1 - 2025
N2 - This company manufactures faucets and sanitary ware in Lima, Peru. This study will focus on the faucet product line. This research focuses on studying a company within the metal-mechanic sector that faces productivity issues, negatively impacting its competitiveness. Periodic visits to the company were conducted to collect data. Various tools, such as “5 Whys”, Ishikawa diagram and Pareto diagram, were employed to identify the main issues, revealing significant problems such as poorly optimized workstations, low-quality parts, high unproductive times and improper machine usage, among others. The root causes were identified to address them using Lean Manufacturing tools, including 5S, Work Standardization, ergonomic analysis and Poka-Yoke. Improvements were simulated using Arena software, yielding remarkable results, such as a 24% reduction in human errors per quarter, an 11.11% increase in productivity, and a 5% reduction in non-productive times. Finally, the profitability of the proposal was evaluated through a Net Present Value (NPV) of 1,792,845.45 USD, an Internal Rate of Return (IRR) of 66.56%, and a return on investment within less than 1.5 years.
AB - This company manufactures faucets and sanitary ware in Lima, Peru. This study will focus on the faucet product line. This research focuses on studying a company within the metal-mechanic sector that faces productivity issues, negatively impacting its competitiveness. Periodic visits to the company were conducted to collect data. Various tools, such as “5 Whys”, Ishikawa diagram and Pareto diagram, were employed to identify the main issues, revealing significant problems such as poorly optimized workstations, low-quality parts, high unproductive times and improper machine usage, among others. The root causes were identified to address them using Lean Manufacturing tools, including 5S, Work Standardization, ergonomic analysis and Poka-Yoke. Improvements were simulated using Arena software, yielding remarkable results, such as a 24% reduction in human errors per quarter, an 11.11% increase in productivity, and a 5% reduction in non-productive times. Finally, the profitability of the proposal was evaluated through a Net Present Value (NPV) of 1,792,845.45 USD, an Internal Rate of Return (IRR) of 66.56%, and a return on investment within less than 1.5 years.
KW - 5S
KW - Ergonomic Analysis
KW - Lean Manufacturing
KW - Metalworking
KW - Productivity
UR - https://www.scopus.com/pages/publications/105019312014
U2 - 10.18687/LACCEI2025.1.1.409
DO - 10.18687/LACCEI2025.1.1.409
M3 - Articulo (Contribución a conferencia)
AN - SCOPUS:105019312014
T3 - Proceedings of the LACCEI international Multi-conference for Engineering, Education and Technology
BT - Proceedings of the LACCEI international Multi-conference for Engineering, Education and Technology
A2 - Petrie, Maria M. Larrondo
A2 - Texier, Jose
A2 - Matta, Rodolfo Andres Rivas
PB - Latin American and Caribbean Consortium of Engineering Institutions
T2 - 23rd LACCEI International Multi-Conference for Engineering, Education and Technology, LACCEI 2025
Y2 - 16 July 2025 through 18 July 2025
ER -